THE PROBLEM
The trade effluent pit was suffering from degradation and as part of the planned site upgrade works a suitable tank lining solution was required.
The trade effluent pit was suffering from degradation and as part of the planned site upgrade works a suitable tank lining solution was required.
With the pit being below ground we proposed the application of Sikagard®-7000 CR. This system offers the following benefits;
Initially the pit was prepared by method of high pressure water jetting using our 10,000 psi jetting unit to ensure excellent adhesion of the new tank lining.
All surfaces were primed using Sikagard® M 790 highly damp tolerant polyurethane primer by method of brush and roller. Because of the short duration of the shutdown it was not possible to make good the substrate using cementitious materials. Instead a repair mortar was made by mixing Sikagard® M 790 with blended kiln dried quartz. This was applied into the tacky primer by trowel to provided a continuous surface suitable for tank lining application.
The first coat of Sikagard® M 790 was applied by method of brush and roller in a red colour
The second coat of Sikagard® M 790 was then applied by method of brush and roller in a grey colour as per best tank lining practice
As per our standard tank lining quality assurance the cured coating was checked for pin holing using a DC Holiday spark tester as a single pin hole is a point of tank lining failure which will allow aggressive chemicals to reach the substrate and attack recommence.
Any pin holes identified were marked prior to making good using the same material applied by brush.
The entire project was completed in less than a week within the client tight shutdown programme.